Bristol 188
The Bristol 188 was a supersonic research aircraft built in the 1950s.
Bristol gave the project the type number 188, of which three aircraft were to be built, one a pure test bed and the other two (constructor numbers 13518 and 13519) for flight testing.Serial numbers XF923 and XF926 were given on 4 January 1954 to the two that would fly. To support the development of the Avro 730 Mach 3 reconnaissance bomber, another three aircraft were ordered (Serial Numbers XK429, XK434 and XK436). The follow-up order was cancelled when the Avro 730 programme was cancelled in 1957 as part of that year's review of defence spending. The 188 project was continued as a high speed research aircraft.
The advanced nature of the aircraft meant that new construction methods had to be developed. Several materials were considered for construction and two specialist grades of steel were selected: a titanium-stabilized 18-8 austenitic steel and a 12%-Cr steel used in gas turbines. These had to be manufactured to better tolerances in sufficient quantities for construction to start. The 12% chromium stainless steel with a honeycomb centre was used for the construction of the outer skin, to which no paint was applied.
The specification required engine installations which permitted the fitting of different air intakes, engines and propelling nozzles.The 188 was intended to have Avon engines but the half ton lighter each Gyron Junior was substituted in June 1957, meaning the engines were mounted further forward with longer nacelles and jet pipes.
The Gyron Junior was under development for the Saunders-Roe SR.177 supersonic interceptor and incorporated a fully variable reheat, from idle to full power, the first such application used in an aircraft.This choice of powerplant resulted in the 188 having a typical endurance of only 25 minutes, not long enough for the high-speed tests required.
In May 1960, the first airframe was delivered to the RAE at Farnborough for structural tests – loading tests both heated and unheated – before moving on to RAE Bedford. XF923 undertook the first taxiing trials on 26 April 1961, although due to problems encountered, the first flight was not until 14 April 1962. XF923 was intended to remain with Bristol for its initial flights and evaluation before turning it over to the MoA. XF926 had its first flight, using XF923s engines, on 26 April 1963. XF926 was given over to RAE Bedford for its flying programme. Over 51 flights, it managed a top speed of Mach 1.88 (1,440 mph at 36,000 ft (11,000 m). The longest subsonic Bristol 188 flight was only 48 minutes in length, requiring 70% of the fuel load to be expended to attain its operational altitude.
The project suffered a number of problems, the main being that the fuel consumption of the engines did not allow the aircraft to fly at high speeds long enough to evaluate the heating of the airframe, which was one of the main research areas it was built to investigate. Combined with fuel leaks, the inability to reach its design speed of Mach 2 and a takeoff speed at nearly 300 mph, the test phase was severely compromised.
The announcement that all development was terminated was made in 1964, the last flight of XF926 taking place on 12 January 1964. In total the project cost £20 million. By the end of the programme, considered the most expensive to date for a research aircraft in Great Britain, each aircraft had to be "cannibalised" in order to keep the designated airframe ready for flight.
XF926 was dismantled and moved to RAF Cosford (without its engines) to act as instructional airframe 8368M, and is preserved at the RAF Museum Cosford.
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